Please use this identifier to cite or link to this item: https://cuir.car.chula.ac.th/handle/123456789/73343
Full metadata record
DC FieldValueLanguage
dc.contributor.advisorParitud Bhandhubanyong-
dc.contributor.advisorAdisak Wangphongsawasd-
dc.contributor.authorPisak Sukondhasingha-
dc.date.accessioned2021-05-12T07:50:28Z-
dc.date.available2021-05-12T07:50:28Z-
dc.date.issued2000-
dc.identifier.isbn9743344322-
dc.identifier.urihttp://cuir.car.chula.ac.th/handle/123456789/73343-
dc.descriptionThesis (M.Eng.) -- Chulalongkorn University, 2000en_US
dc.description.abstractThis thesis is about the study of quality improvement in the production line of crankshaft for compressor refrigerator by reducing the failure from dimensional defects. The improvement increases the effectiveness of production line by lessen the loss from non-conforming product and increase on-time delivery and quality of product. The dimensional defect in production line can be solved by 2 methods, 1) the reduction of continuous defects and 2) the controlling of the deviation of process. In order to reduce the defects in production line immediately and effectively, the implementation plan can be divided into 3 major methods as follow: 1) the improvement in the inspection method during the production process 2) the effective maintenance and 3) the monitoring system to show the states of production line As the result of improved production-processing implementation, the percentage of non-conforming product in production line after improvement was reduced from 5.8 to 3.5.-
dc.description.abstractalternativeThis thesis is about the study of quality improvement in the production line of crankshaft for compressor refrigerator by reducing the failure from dimensional defects. The improvement increases the effectiveness of production line by lessen the loss from non-conforming product and increase on-time delivery and quality of product. The dimensional defect in production line can be solved by 2 methods, 1) the reduction of continuous defects and 2) the controlling of the deviation of process. In order to reduce the defects in production line immediately and effectively, the implementation plan can be divided into 3 major methods as follow: 1) the improvement in the inspection method during the production process 2) the effective maintenance and 3) the monitoring system to show the states of production line As the result of improved production-processing implementation, the percentage of non-conforming product in production line after improvement was reduced from 5.8 to 3.5.-
dc.language.isothen_US
dc.publisherChulalongkorn Universityen_US
dc.relation.urihttp://doi.org/10.14457/CU.the.2000.58-
dc.rightsChulalongkorn Universityen_US
dc.subjectCranks and crankshafts -- Quality controlen_US
dc.subjectAssembly-line methodsen_US
dc.subjectProduction controlen_US
dc.titleQuality improvement for the production line of crankshaften_US
dc.title.alternativeการพัฒนาคุณภาพสำหรับสายงานการผลิตเพลาข้อเหวี่ยงen_US
dc.typeThesisen_US
dc.degree.nameMaster of Engineeringen_US
dc.degree.levelMaster's Degreeen_US
dc.degree.disciplineEngineering Managementen_US
dc.degree.grantorChulalongkorn Universityen_US
dc.email.advisorNo information provided-
dc.email.advisorNo information provided-
dc.identifier.DOI10.14457/CU.the.2000.58-
Appears in Collections:Eng - Theses

Files in This Item:
File Description SizeFormat 
Pisak_su_front_p.pdfหน้าปก บทคัดย่อ และสารบัญ815.57 kBAdobe PDFView/Open
Pisak_su_ch1_p.pdfบทที่ 1839.44 kBAdobe PDFView/Open
Pisak_su_ch2_p.pdfบทที่ 2948.64 kBAdobe PDFView/Open
Pisak_su_ch3_p.pdfบทที่ 31.89 MBAdobe PDFView/Open
Pisak_su_ch4_p.pdfบทที่ 41.28 MBAdobe PDFView/Open
Pisak_su_ch5_p.pdfบทที่ 51.12 MBAdobe PDFView/Open
Pisak_su_back_p.pdfรายการอ้างอิงและภาคผนวก1.34 MBAdobe PDFView/Open


Items in DSpace are protected by copyright, with all rights reserved, unless otherwise indicated.